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2012年10月26日星期五
USCID conference on Benchmarking Irrigation System Performance Using Water Measurement and Water Balances.
----------------------- Page 1-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
MODERNIZING IRRIGATION FACILITIES
AT SUTTER MUTUAL WATER COMPANY: A CASE STUDY
1 2 3
Frederick F. Schantz , Stuart W. Styles , Beau J. Freeman ,
4 5
Charles M. Burt , Douglas Stevens
ABSTRACT
In 1999 Sutter Mutual Water Company (SMWC) began an effort to modernize its
water-distribution system in an attempt to reduce operation and maintenance costs
and conserve water and power resources. The primary technical support was
provided by professionals from the Irrigation Training and Research Center
(ITRC), California Polytechnic State University (Cal Poly), San Luis Obispo.
Additional technical expertise was provided by Concepts in Controls of Visalia,
California and Wilson Pumps of Woodland, California. This modernization
project was partially funded by the United States Bureau of Reclamation (USBR),
Mid-Pacific Region, Northern Area Office, through a Field Services Program
Grant and technical support agreement with the ITRC.
The effort encompassed two projects within the company’s service area located
within the boundaries of California’s largest reclamation district, Reclamation
District 1500. The projects were (1) the automation of the pumping plant at
Portuguese Bend with a new Variable Frequency Drive (VFD) pump and
Supervisory Control and Data Acquisition (SCADA) system and (2) the
demonstration of new SCADA-compatible electronic flow measurement
technologies for both canals and pipelines.
The anticipated, and ultimately realized, benefits of the modernization effort was
a savings to the company due to a reduction in the amount of water diverted,
power consumed and number of personnel required to operate and maintain its
system.
1 Operations Manager, Sutter Mutual Water Company (SMWC), P.O. Box 128, Robbins,
CA 95676. ffschantz@aol.com
2 Director, Irrigation Training and Research Center (ITRC), California Polytechnic State
University (Cal Poly), San Luis Obispo, CA 93407. sstyles@calpoly.edu
3 Senior Irrigation Engineer, ITRC, Cal Poly, San Luis Obispo, CA 93407.
bfreeman@calpoly.edu
4 Professor and Chairman, ITRC, Cal Poly, San Luis Obispo, CA 93407.
cburt@calpoly.edu
5 President, Concepts in Controls, 225 S. Cotta Ct. Visalia, CA 93292.
dougstevens@MSN.com
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 2-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
INTRODUCTION
Sutter-Mutual Water Company (SMWC), a farmer-owned, non-profit water
company, decided in 1998 to begin modernizing its irrigation facilities in an
attempt to reduce its increasing operation and maintenance costs while conserving
water and power resources. The following paper is a 1999-2001 status report on
what has become an ongoing effort.
The work completed to date has been possible due to a coordinated effort between
company personnel and professional engineers from the Irrigation Training and
Research Center (ITRC), California Polytechnic State University (Cal Poly), San
Luis Obispo, Concepts in Controls, Visalia, California and Wilson Pumps,
Woodland, California. This modernization project was partially funded by the
United States Bureau of Reclamation (USBR), Mid-Pacific Region, Northern
Area Office, through a Field Services Program Grant and technical support
agreement with the ITRC.
Background
For over 80 years the company has operated and maintained its irrigation
facilities, initially using mostly vintage technology, which has proven to be very
reliable. In the 1960-1970s, three new pumping stations were built and more
efficient turbine pumps were installed to help reduce power consumption and to
increase water diversion efficiency. For economic and operational reasons, in
1999 it was decided to begin installing additional technology in some of the plants
in order to take advantage of the substantial savings offered by such technology.
The first equipment chosen by the company was a Variable Frequency Drive
(VFD) unit and a Supervisory Control and Data Acquisition (SCADA) system,
which were installed in the Portuguese Bend plant during 1999-2001. While this
project was being completed a second project was also initiated in order to
measure flows in two different canals. Both of these projects are described
below.
Description of Company
Formed in 1919, SMWC is one of the first water companies to be established in
the state of California. The company’s physical location (Figure 1) is
approximately 45 miles northwest of Sacramento, California and is bordered in
the north by the Tisdale Bypass, in the west by the Sacramento River and in the
east by the Sutter Bypass. The southern boundary is located at the southern end
of Sutter County near the Fremont Weir where the Sacramento River and Feather
River come together. The company’s 46,746 irrigable acres (18,917 ha), which
are part of the 67,850 (27,470 ha) gross service area that is maintained by
Reclamation District 1500 flood control and drainage personnel, are served by
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 3-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
approximately 400 turnouts. Approximately 200 miles (322 km) of canals and
laterals in the distribution system convey water to the fields.
Figure 1. Map of Sutter Mutual Water Company service area
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 4-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
PROJECT #1: INSTALLING A VFD UNIT AND SCADA SYSTEM AT
THE PORTURGUESE BEND PUMPING PLANT
In early 1999 the company decided to proceed with the installation of a Variable
Frequency Drive (VFD) unit and a Supervisory Control and Data Acquisition
(SCADA) system in the pumping plant at Portuguese Bend (Figure 2) following
an explanation of the technology by ITRC staff who detailed the work to be done,
the equipment to be used and the cost and benefits of the project. The VFD, in a
manual mode, was successfully installed by the end of the year after three unique
problems critical to the successful operation of the new technology were
identified, evaluated and resolved: (1) an adequate radio signal between the office
and field site, (2) proper siphon breaker operation, and (3) adequate cooling of the
VFD unit. A description of the VFD and SCADA system is as follows.
The Variable Frequency Drive (VFD) Unit
Constant-speed AC motors drive many pumps used for water distribution and
delivery at the district or grower level. When flow control is needed to
accommodate changes in downstream demand, typically two methods are
employed to control the flow rate and pressure: (i) a downstream throttling valve
is used to alter the system curve, and (ii) some of the output is by-passed back
into the intake.
Figure 2: Portuguese Bend Pumping Plant on the Sacramento River
With these two methods a considerable amount of energy could be wasted in
doing work that is not needed just to achieve the desired flow rate. VFD units
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 5-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
provide an effective way of reducing the speed of the pump drive motor, thereby
allowing the flow rate or pressure to be adjusted to the desired level without the
additional energy from throttling or by-passing. Basically the VFD is an
electronic device that is used in conjunction with a constant-speed AC motor.
The VFD accepts the standard line voltage and frequency then converts the signal
into a variable frequency and voltage output that allows the standard constant-
speed AC motor to be varied in speed.
Advantages of a VFD: VFDs provide the potential for system automation of
pumping plants such as Portuguese Bend. Water level sensors can be used as
feedback into the controller to continuously adjust the VFD speed for varying
downstream conditions. In general, this permits the ability to provide water
deliveries to growers on-demand. In turn, growers are able to schedule irrigations
to match the crop water requirements rather than district limitations. This type of
VFD operation also offers the potential for labor savings over manual adjustment.
The further advantages of VFD systems include the following:
• Softer starting: the device limits the current inrush to the motor providing
for a smooth non-shocking acceleration of the pump shaft speed up to its
operational RPM
• Elimination of pressure surge: bringing the system up to operating speed
slowly removes the pressure surge caused by an almost instantaneous
acceleration of the water to its operational flow rate
• Reduction of operating costs: by reducing the energy input over previous
control methods (by-pass) operating costs can be reduced
• Reduction of motor stress: reduces mechanical stress on motor windings
• Reduction of peak demand charges: by reducing the energy loads the
overall peak demand of the facility can be reduced
Disadvantages of a VFD: There are important issues to consider when VFD
devices are being used, as follows:
• Increased motor stress: electrical stress increased due to the steep voltage
wave that forms in the power supplied by the inverter. Older motors with
inferior insulation may have problems. Typically the motor should be
dipped and baked twice. Newer VFDs that include “soft switching output
technology” can significantly reduce motor stress and interference from
harmonics.
• Increased maintenance: while VFD units are very reliable they are an
additional item requiring maintenance. In critical applications, it is
essential to have spare parts and maintenance expertise or retain the ability
to by-pass.
• Harmonics concern: with the increasing number of control systems going
on-line, the line interference produced by some VFD units can cause
problems.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 6-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
• Environmental conditions: most units require relatively dust free
enclosures with some type of temperature control. Most of the pumping
VFD applications can utilize a simple water-to-air radiator type cooling
system (simple and effective).
Energy Savings: VFD units usually reduce pumping costs by reducing the pump
drive motor speed to match the desired operating conditions thereby reducing
energy input. Without a VFD device this is typically accomplished by using
either a by-pass set-up or a downstream throttling valve. The system layout for a
typical by-pass installation consists of a pump and by-pass piped into a standtank.
With this arrangement the by-pass maintains a constant head in the standtank
regardless of flow, as there is less downstream demand. The excess flow is by-
passed to the pump intake to maintain a constant head in the standtank or canal.
Determining how a pump will operate in a given situation requires an
understanding of the pump and system curve. The pump characteristic curve for a
standard centrifugal pump shows that the pump, at a fixed speed, has a flow rate
associated with a particular pressure; high flow, lower pressure vs. low flow,
higher pressure. The intersection of the pump curve and the system curve shows
the point of system operation.
If, instead, the pump speed is modified using a VFD device to control head just
below the by-pass, flow and head are reduced together along the system curve. A
comparison of the relative pump water horsepower with (i) VFD, and (ii) by-pass
installations are shown by the shaded areas in Figure 3.
e
r Reduced Speed e
u r
s u
s s
e s Reduced Speed
r e
P r
P
d
a d
e a
H e
H
Static head or Lift Static head or Lift
Flow Desired Flow Unthrottled Flow Desired Flow Unthrottled
No By-pass No By-pass
Figure 3. Water horsepower (shaded area) for pumping plant with (i) VFD and
(ii) by-pass
However, the water horsepower differences above are only some of several
factors to consider. To properly compare the actual cost savings of a VFD
system, the overall plant pumping efficiencies with and without the VFD device
also need to be considered. The major additional losses that must also be
considered in determining the overall pumping plant efficiency are as follows:
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 7-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
• As the system curve changes or the pump speed is reduced, the
operating efficiency of the pump changes. Therefore, for each
operating point the pump efficiency must be checked.
• VFD units have some losses associated with the conversion process to
the new operating frequencies. In general the units are relatively
efficient, 95%. But, as the frequency is lowered, some units do
become less efficient. The individual specifications for the VFD being
considered should be obtained.
• Electric motors if sized properly near maximum loading, can be very
efficient. With VFD units used in pumping, the motor loading is
reduced as the speed is reduced. This reduction in motor loading can
reduce its efficiency and drive motor losses will result.
• Drive friction losses can be reduced with VFD applications. As the
speed is reduced the mechanical friction on drive shaft components is
reduced.
In addition to the items above, it is important to consider the relative volume
pumped each season. Small pumping volumes generally produce small savings
and do not justify VFD installations.
Cost Savings Analysis: To determine the total savings due to the VFD unit, a
detailed cost savings analysis was begun on the VFD installation on pump #1
(100 hp motor) at the Portuguese Bend pumping plant. Initial savings have
already been realized with the reduction of one employee who was needed to
constantly monitor and reset the plant’s three pumps as dictated by flow
requirements out of the plant’s main canal. The main costs now under evaluation
involve two other components as follows: (1) energy savings as a result of
eliminating the by-pass practice (before meter) to control delivery flow, and (2)
reduction of spilled water out of the canal, which reduces metered pumping of a
purchased volume, plus the additional energy savings associated with the
reduction in pumped volume. Both portions of the savings analysis do not take
into consideration the specific time of use rates; they are based on the total
monthly values. The reduction in canal spill and the associated energy savings
are only achievable with the new SCADA system.
Table 1 shows the expected estimated annual energy savings based on the reduced
pumping costs associated with a VFD unit. The cost savings analysis is based on
an estimate of the average pumping costs before and after the installation of a
VFD unit. In addition, an estimate of the average pumping cost with a VFD using
a simple control algorithm is included to illustrate the expected additional cost
savings during the first year operating with the new SCADA system. Table 2
shows the anticipated annual savings of approximately $2,000 to the company on
Portuguese Bend’s main canal due to the reduction in spilled water along the
canal. Total cost savings from reducing both canal spill and from overall energy
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 8-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
cost savings should be between $14,000 and $18,000 per year and will increase
even more in the future as energy costs continue to increase.
Table 1. Average annual energy savings expected from VFD operations
Pumping Annual Energy Annual Energy
Cost Savings based on Savings based on
Item $/AF 6,000 AF/ Season 8,000 AF/ Season
without VFD 4.7 --- ---
with VFD 3.0 $10,200 $13,600
with VFD and
2.7 $12,100 $16,200
simple algorithm
Table 2. Average annual savings anticipated from a reduction in Portuguese Bend
canal spill with the new VFD and SCADA system
Description Amount
Approximate annual spill at end of canal (acre-feet) 200
Possible reduction in spill with VFD (acre-feet) 120
Water value as missed opportunity to sell ($/acre-feet) $12.00
Possible revenue from missed sales annually ($) $1,440
Approximate pumping cost $/acre-feet (from pump test data) $4.18
Energy savings from reduced pumped volume ($) $502
Total Anticipated Canal Spill Savings $1,942
The SCADA System
Overview: The basic objective of the automation at Portuguese Bend was to vary
the pump flow rates from the pumping plant in order to maintain a target water
level in the canal. This required the integration of a VFD unit at the pumping
plant and a new SCADA system. Specifically, this involved the ability to
remotely monitor the system (water levels, flow rates, pumps on/off, etc.),
manually control operations from SMWC’s administration office, and to
eventually control the system automatically using the new VFD unit. This
required the integration of data acquisition components (sensors for water level,
electronic flow meters, etc.) with computerized controllers for implementing
supervised commands. Monitoring and controlling operations at a remote site
such as Portuguese Bend further required a two-way communications network
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 9-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
between the remote office location and the control site. Such a system is often
referred to as a Supervisory Control and Data Acquisition (SCADA) system.
SCADA is a tool that allows irrigation companies or districts to acquire real-time
information and control operations at remote sites from a central location, usually
in the main office or at an operations center. By having this real-time information
available at the office, the system can also be managed on a real-time basis,
thereby providing the ability to achieve maximum water conservation and
operational flexibility.
In the water industry, the SCADA systems installed just a few years ago were
one-of-a-kind systems custom designed for a specific job. As a result, these
systems were not in most cases industrially hardened. Their relatively short-term
design efforts did not address all of the day-to-day conditions the components
would be subjected to. Consequently, system reliability was low. In addition, the
communications protocols were all unique within these proprietary systems;
therefore, no interchangeability between components and different vendors was
possible. The overall communication systems used also added to the unreliability
of early SCADA systems. The older systems typically used lower frequency
voice radios for data transmission that were prone to many outside disturbances.
Current SCADA systems are now being designed under a term called “open
architecture”. This new approach uses off-the-shelf industrially hardened
components, which can be linked together using common communication
protocols. One such protocol currently adopted by the industry is Modbus. The
current systems configuration assembles individual components, called Remote
Terminal Units (RTU’s), to control or monitor at each site independently. These
standard components are then configured (programmed) for the specific task. The
site RTU information is then linked back to the central location via radio
communication. The open architecture and industrially hardened components
have allowed increased scalability and reliability.
Radio communication for the SCADA systems has also improved. Equipment
and FCC regulations have allowed the operation frequencies to increase, thereby
improving reliability. One notable advance in radio communication has been the
FCC approval of a technology known as Spread Spectrum radio. This is an
unlicensed 900 Mhz frequency ‘hopping’ technique that provides reliable
communication within about a 15-mile range. The range can be extended with a
repeater configuration.
Project Phases: Due to the complex nature of installing a SCADA system into an
irrigated area, successful implementation is best accomplished in phases.
Initiating change in the routine operation of key facilities and altering the day-to-
day activities of company or district personnel can create significant uncertainty.
It is therefore necessary that this uncertainty is addressed during each step of the
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 10-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
process and a level of confidence is gradually built-up in the participants.
Achieving this critical “buy-in” from the people who will actually use the system
is essential for the success of modernization projects. This phased approach has
the important benefits including maximizing reliability while allowing an
irrigation company or district to prioritize critical modernization needs and
implement components on a site-by-site basis. Styles et al. ( 1999) outline further
advantages of the phased approach based on experience in modernization projects
in irrigation districts. The Project Phases used for installing a SCADA system for
SMWC were as follows:
Phase 1 (Completed in April 2001): The first phase of the SCADA part of the
project was to install, test and calibrate a new water level sensor in the head of the
main canal at Portuguese Bend. The new sensor located in a stilled area at the
start of the canal was connected to the RTU/PLC at the Portuguese Bend pumping
plant. The new sensor installation was setup so that water levels in the canal were
measured once per second and transmitted via radio to the RTU/PLC, where it
was stored in a data table and averaged over a one-minute time interval. Upon
completion of this task, the Lookout® screens at the district office included
information on the canal water levels at two locations, the river stage, the status of
each pump (on/off and speed) and target depth (water level setpoint). In addition,
the Lookout® screens were configured so that the target depth could be remotely
changed from the office (for future automatic control), and so that up to
15 coefficients used for the distributed automatic control could be remotely
changed from the office. However, the ability to change these coefficients were
“hidden” so that only authorized personnel will be able to change the values.
Phase 2 (Completed in June 2001): This was the first step toward automating the
site but nothing automatic was introduced at this stage. The VFD pump was
tested on-site in manual mode with occasional remote manual operation. Manual
VFD operation means the operator sets the motor speed control using the percent
speed control located in the pumping plant. This phase facilitated testing of the
new communications equipment, sensors, VFD controls, connection to the office
computer, a new air/vacuum relief valve, etc.
Phase 3 (Completed in October 2001): This was the second step toward
automating the site. There was a continuation of the remote manual mode of
operation, but it was expanded to include a new flow meter. Rather than using
only water levels as feedback, the operators now had information on specific flow
rates at the pumping plant. A new electronic flow measurement device
(Panametrics acoustic meter) was installed on one of the three pumping units and
the flow rate was available to the operator. The digital display screens for the
new Panametrics meters are shown in Figure 4. This did not mean that operators
were expected to make hourly changes from the remote office location. This step
required at least two months of operational testing extending into the peak
irrigation season.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 11-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
Phase 4 (Completed in December 2001): This was the third and final step of
automating the Portuguese Bend pumping plant. A Proportional-Integral-Filtered
(PIF) algorithm for control of the site was programmed into the RTU/PLC and
implemented. The control algorithm was a PIF algorithm supplied by the ITRC
and not the internal Proportional-Integral (PI) equation supplied by the VFD’s
manufacturer.
The Lookout® screens in the office necessary to support this automation were
already in-place. The ladder logic and additional site programming were
completed during this stage. At this time the effect of fluctuations in the
Sacramento River level was factored in and added to the ladder logic
programming, allowing the minimum VFD speed to shift with the river level.
The Lookout® screens were modified to allow a person in the remote office
location the ability to shift the pumps to automatic or manual control. In the case
of remote manual control, this meant the ability to control the speed of the VFD
and the number of pumps operating from the office. This final step allowed for
the fullest possible (or desirable) automation of the site.
Figure 4. Digital display screens for new Panametrics flow meters inside the
Portuguese Bend pumping plant
CANALCAD Modeling: During the modernization effort, the ITRC completed
several unsteady flow hydraulic simulations of the first pool of the Portuguese
Bend canal were conducted to determine the optimum control scheme for the new
VFD unit. The algorithm uses PIF control logic based on water depth
measurements 1,800 feet downstream of the Portuguese Bend pumping plant.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 12-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
The algorithm controls that water depth using the VFD and single stage pumps in
the pumping plant.
The following is the control logic with optimized algorithm parameters:
VFD pump speed change: DS =1.3 * Round (DQ, 3)
Required flow rate change: DQ=35.315*[KP*(FE1-
FE2)+(KI*FE1)]
with: FE1 =fc*FE2+(1-fc)*ENOW
FE2 = FE1 of previous step.
KP = -6.50
KI = - 0.18
fc = 0.84
Simulation Results: Figure 5 summarizes the best modeling results and algorithm
for controlling the water depth about three-quarters of the way downstream from
the Portuguese Bend canal.
Sutter Mutual Water Co. Portugese Bend Pumping Plant (CC STN 1+00)
PB_20RT5.ccd, PB_20RT5.xls, PB_PIF1.FOR
6 250
Water depth MTx3 2300 feet d/s of pumps KP = - 6.5
yt
KI = - 0.18
Water depth MTx2 1800 feet d/s of pumps 225
Water depth at immediately d/s of pumps fc = 0.84
5 Pumping plant flow(cfs)
200
175 )
S
4 F
C
(
e
150 t
a
) R
t
f w
(
o
h l
t 3 125 F
p
e t
n
D a
l
r P
e
t 100 g
a
n
W i
p
2 m
u
75 P
- Control of pumping plant is based on transducer 1800 feet d/s of pumps with the
50
1 goal of controling a 3.4' depth at that location
- CanalCAD v2.04 simulation uses 1 sec computational TS with 1 min control TS
based on the average of 60 "yest" values 25
- TO flow change ramp time =absolute(flow rate change)*(5min/10CFS), output
generated every 6 sec
0 0
0:00 6:00 12:00 18:00
Time (h)
Figure 5. Water level control results when turnout flow changes occur at a rate of
5 minutes for every 10 cfs change
The control action occurs once a minute based on the average of at least
60 measurements of water depth. The graph presents the control results for nine
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 13-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
simulated end-of-canal turnout flow changes that range from 5 to 110 cfs and that
occur over an 18-hour period. The turnout flow changes occurred based on five
minutes per every 10 cfs change in flow.
The graph shows the following information:
− Water depth immediately downstream of the pumping plant,
− Target water level of 3.4 ft at 1,800 ft downstream of the pumping
plant,
− Water depth at 1,800 ft downstream of the pumping plant,
− Water depth at 2,300 ft (end of the pool), and
− Pumping plant flow rate
Figure 5 demonstrates satisfactory water level control with frequent flow rate
changes over a relatively short period of time using the ITRC selected control
6
algorithm. The target water level to maintain is 3.4 ft and the control location is
1,800 ft downstream of the pumping plant. This is the location of two transducers
7
for measuring water depth .
VFD Documented Response and CanalCAD Results
Sutter-Mutual Water Company, Portuguese Bend
December 11, 2001
7.5 80
Actual water depth 1800 feet d/s of pump, ft
Predicted water depth 1800 feet d/s of pump, ft
7.0 Water level target = 5.6 ft 70
Approximate demand flow rate, cfs
VFD pump speed, %
6.5 60
Predicted water level
from CanalCAD
% s
6.0 50 f
, c
p ,
t e
f
m t
, u a
h
t P R
p
e 5.5 40 D w
D F o
l
r V F
e
t Actual water level
a
W
5.0 30
4.5 20
Demand flow changed from 20 cfs
4.0 10
to 4 cfs at 9:05
3.5 0
7:45 8:00 8:15 8:30 8:45 9:00 9:15 9:30 9:45 10:00 10:15 10:30 10:45
Time
Figure 6. Documented VFD response, water level control results and predicted
water depth with an 80% change in demand flow
6 The target water level was later changed to 5.6 ft after the canal was de-silted
and the sensor height adjusted.
7 A redundant measurement (Y2) is used to check the integrity of the (Y1)
measurement, which is used in the control logic.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 14-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
Documented VFD Response: The documented response of the Portuguese Bend
pumping plant from field tests conducted in December 2001 is shown above in
Figure 6. During the final evaluation, the demand flow was varied with multiple
flow rate changes to test the response time, stability and robustness of the VFD
and SCADA systems. The flow changes were made manually by the operator
adding or removing weir boards and opening or closing the gate at the check
structure located at the downstream end of the first pool of the Portuguese Bend
canal.
PROJECT #2: ELECTRONIC WATER FLOW MEASUREMENT
The second project of the modernization program at the SMWC was the
successful utilization of advanced flow measurement technologies. Accurate flow
measurement is an integral part of the scientific management of water and energy
resources. New electronic flow measurement devices provide a cost-effective and
practical means to precisely measure flows at critical locations such as the
pumping plant at Portuguese Bend. Panametrics, SonTek Argonaut™ SL and
Unidata Starflow ultrasonic flow meters were used to determine flow rates and
volumetric flow in the discharge pipeline and canal at Portuguese Bend in
conjunction with the evaluation of the new VFD and SCADA system. A brief
overview of the deployment of these devices is presented in the following
sections.
Testing in the Portuguese Bend Pumping Plant’s Main Canal
The new VFD pump permits excellent control of the water level in the first pool
of the canal by allowing an unlimited flow rate range. However, in order to
correctly program the RTU/PLC of the VFD, the relationship between “change in
pump speed” and “change in flow rate” must be known. In practice, this is
neither a constant nor a precisely known value. The ITRC used ultrasonic flow
measurement equipment on the VFD pump discharge pipeline and pump affinity
laws to estimate the relationship between pump speed and flow rate. A
Panametrics acoustic flow meter was installed on the VFD pump discharge
pipeline in order to integrate real-time flow data into the new SCADA system, in
addition to providing flow rate via a digital display in the pumping plant (refer to
Figure 4).
Testing in the Tisdale Pumping Plant’s Main Canal at the Tisdale Bridge
A SonTek Argonaut™ SL Doppler current meter (Figure 7) was deployed in the
Tisdale main canal near Tisdale Bridge from April 18 to July 31, 2001. The canal
flow rate was measured in 10-minute intervals and the daily flow volume was
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 15-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
calculated. The daily flow volume measured by the SonTek Argonaut™ SL was
compared to data provided by SMWC. Drawings of the canal cross-sections at
the deployment location were prepared and used in the calculation of volumetric
flows. The Tisdale Bridge location is shown in Figure 7 below.
Figure 7. SonTek Argonaut™ SL Doppler current meter at Tisdale Bridge
The percent difference in the measured volume of delivered water ranged from
1.4 to 2.6% per month while the percent difference in total delivered volumes
during the four months was less than one percent (–0.9%) as shown in Figure 8.
In both monthly and total volumes, the meter registered the slightly higher
amount.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 16-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
Sutter-Mutual Water Company, Tisdale Bridge
SonTek Argonaut SL and River Diversions
April to July, 2001
1,6 00
1,4 00
1,2 00
t
f
-
c 1,0 00
a
,
e
m 8 00
u
l
o
V
6 00 SonTek Volumetric Flow, ac-ft
w
o
l
F 4 00 Sutter-Mutual River Diversions, ac-ft
2 00
0
4/18 /2 00 1 4/28 /2 00 1 5/8/20 01 5/18/20 01 5/2 8/20 01 6 /7/20 01 6/17/20 01 6/27/20 01 7/7/2 00 1 7/17/20 01 7/27/20 01
Irrigation Day
Figure 8. Comparison of Sutter Mutual Water Company and the SonTek
Argonaut SL volumetric flows at Tisdale Bridge
Testing at Portuguese Bend Canal
To facilitate the final evaluation testing of the VFD and SCADA system at
Portuguese Bend, a Unidata Starflow acoustic Doppler flow meter (Figure 9) was
installed in the canal approximately 200 ft downstream of the pumping plant. The
Unidata Starflow ultrasonic flow meter provided the total flow rate from the
pumping plant during the test period. This was necessary because the new
Panametrics meter had not yet been installed on pump #3 (single stage) at the
pumping plant. The Unidata Starflow meter was field calibrated using the
Panametrics flow meter on pump #1.
Irrigation Training and Research Center (ITRC) – www.itrc.org
----------------------- Page 17-----------------------
Presented at the July 9-12, 2002 USCID conference on Benchmarking Irrigation System Performance Using
Water Measurement and Water Balances. San Luis Obispo, CA.
http://www.itrc.org/papers/modernsmwc/modernizingsmwc.pdf ITRC Paper No. P02-004
Figure 9. Digital display LCD screen on the Unidata Starflow acoustic Doppler
flow meter
SUMMARY
In summary, the modernization effort at SMWC is still continuing in the year
2002 when the company hopes to install a SCADA system in its Tisdale pumping
plant. Savings resulting from the installation of the VFD and SCADA system at
the Portuguese Bend pumping plant are being closely monitored and already have
shown important benefits to the water company and reclamation district as a
whole, especially in the area of conserved water and reduced energy costs.
REFERENCES
Styles, S.W., C.M. Burt, M. Lehmkuhl, and J. Sweigard. 1999. Case Study:
Modernization of the Patterson Irrigation District. Presented at the USCID
Workshop on Modernization of Irrigation Water Delivery Systems. Oct. 17-21,
1999. Phoenix, Arizona.
Irrigation Training and Research Center (ITRC) – www.itrc.org
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